So at VIR in late March, I ran my first event with my newly refreshed engine. At first it went like stink. Until it didn’t. I had a used engine in after I lost this one last summer, and refreshed lots of parts with the used engine (cap, rotor, intake boot, hoses as required). So the first session was good, but power cut out hard entering hog pen (downhill right hander) one time. Second session had the same result (not sure where it occurred but it cut out again) but still ran great otherwise. Third session I noticed a rough idle in pit lane, which turned into a dead miss at WOT going on track. Would occasionally clear out at ~5500 RPM+ but generally not. After cooling off awhile, it was slightly better (slightly less than continuous miss at WOT) on the out-lap, but then the same symptoms resumed within 1 lap. Trackside troubleshooting had us suspecting a fuel injector because one plug (#2) was wet and black while the others showed lean. Changing plug and testing, then ignition wires and testing had no effect. Sometimes it would clear up but always returned. Loaded on trailer the next day and it missed terribly (possibly more than 1 cylinder miss) such that it stalled at near WOT pulling on the trailer. Strongly suspected the #2 injector at this point.
At home, rolled it off the trailer and into the shop without starting. All plugs showed black, so single injector less likely. Tested everything on ECU harness connector and everything checked out per Bentley manual specs. Coil resistance measured out of spec (7.39k ohms instead of 5k+or-1k spec). ECU temp sensor was slightly (<10%) out of the allowed range at 70F per the Bentley manual. Checked injector resistance, all checked out. Replaced injectors, assuming that one had been plugged. No change. Checked fuel pressure, and it checked out (~43.5 psi with engine off, manually running fuel pump and ~40 psi at idle). Changed coil with one I had on hand that came from my eta car (same part number) that tested at 5.25k ohms (well within spec). Thought I had it fixed. Pulled onto the trailer fine, took it to the dyno a week later. Oh, during this test process, I pulled the AFM and a used spare I had, and tested it by applying voltage across the terminals and measuring a linearly increasing voltage output with flap angle and no dropouts on both units.
Ran pretty good on the dyno until I did the first actual pull, where it hit 100 hp before starting to miss hard and power dropped to <80 hp, and RPMS wouldn’t climb steadily (thanks to the miss). Measured fuel pressure and observed drops below 40 but this was on overrun, not under load. We didn’t have a wideband O2 sensor in the exhaust for that pull, but afterward it would run really lean while missing. Unfortunately no data on when it was running correctly (however briefly). Suspected fuel pump. Changed fuel pump. No change. Changed fuel pressure regulator. No change, but fuel pressure measured slightly lower and took a little longer to settle back to ~40 psi at idle with new FPR. Changed fuel filter, though it was new prior to the March event. No change.
Thought about the problem and remeasured the crank position sensor. Measured just within spec (540+or-10%, measured 486). My new Hella branded spare measured 471-48x. Changed it and found no difference. Tried my chipped ECU (which I routinely run at hill climbs, so I know it works well). No change. Swapped fuel relay from my eta car. No change. Swapped fuel relay back and swapped main relay with one from eta car. No change. Actually swapped AFMs and aside from a low idle with the other one, no change. Inspected distributor cap (new last summer with the used engine), and aside from slight wear on the cylinder terminals, appeared fine. Center post resistance measured 0.0 ohms. Rotor was also new last summer with the used engine and measured 984 ohms (spec 1000+or-200 ohms). As far as I can tell, the only part(s) I haven’t changed, measured, or measured and subsequently changed are the spark plugs and the engine harness. Just didn’t feel like digging out a set from my spares tonight once 8PM rolled around.
Oh, I should also mention that cylinder compression test at the track measured within 7 psi, and I believe the range was 160-167. Either way the numbers were good and consistent.
I’m looking for any thoughts on anything I might have missed. I’m about to start poring over the schematic for anything I might have missed. Aside from a bad harness, I can’t see what it could be because I consider spark plugs pretty unlikely, especially given our earlier troubleshooting issues. Can anyone weigh in on this?