Scott,
I have a little anecdotal evidence for you regarding re-using stock engine parts. I am having some luck with some (at least in the short term).
We just finished running an event at Sebring and the ambient temps were hot (heat index 110F). The point about the heat is that racing in this heat with stock engines and a factory oil cooler is as tough a duty we can ask of these engines.
It was the first time I had my car on the track in 6 months.
6 months ago in maybe 80F ambient temp I was losing oil pressure in turn 12 (long hard accelerating left hander). The light came on (I don’t have a gauge) and stayed on for about 2 seconds for the last 4 laps or the race or so. It was disconcerting as hell. I was worried that I had damaged the bottom end. So, I sent the oil off to be analyzed and ordered a crank scraper form Chuck Taylor.
Oil analysis came back with normal wear metals
While installing the crank scraper I had my mechanic “inspect” the rod bearings. He pulled off the cap on four of the rods (1,2,5,6) Everything looked like new so he put it back together using the same bearings and same rod bolts. This is a real no no in some books and it had me a bit concerned.
During this same visit to the mechanic we installed a new aftermarket replacement head. Why? My old head had been welded up once already (three broken rocker journals on the intake side. Prior to my owning the car by the way) and the machine shop guy did not feel good about welding and machining this head again. We did use new head bolts. At the same time, we installed newly reconditioned injectors (cores sourced from the junk yard) from RC engineering.
Within the last couple of months the car has been to the dyno twice where we did probably 15 pulls trying to figure out why it was running lean. The point is, 15 pulls in a hot Florida garage is hard work.
As a side note on the lean issue, It looks like it was the reconditioned injectors. The TPS was replaced, the fuel pressure regulator, filter, and pump were all also replaced. We had good fuel pressure at the rail but lousy A/F ratio and 133 hp and 143 ft lbs of torque. After struggling with this and with me at my wits end, at 4:00 Friday afternoon we put the original injectors back in the car and on a leap of faith I put it on the trailer and took it to Sebring. I was determined that I was not going to miss another event at my home track and I was going to use the old butt dyno to determine if the car was running OK.
I was a bit nervous thinking that I had a very lean A/F ratio, a new untested head, re-used rod bolts and bearings, and a new crank scraper so I took it easy the first session. The car still feels a little flat but it is competitive. It is still not as fast as the Black’s car though which has legal HP and torque. I am guessing that mine is now around 150 HP. The crank scraper also did its job as the oil light never flickered.
Time (and continued oil analysis) will tell if re-using the rod bolts/ bearings was a good or bad idea.
Since the car is still slow down the straights, I still have some work to do to get the max HP up. Since this aftermarket head is still an unknown I may still swap the 100K mile motor out of my convertible into the race car. Since you know how to do that now I may invite you down some time next winter to show me and the Blacks how it is done. OK?
Don