(not so)Quick review.
Dec08 Molitor hoses up my perfectly serviceable motor.
Feb09 After freezing my ass off for 4 days staking out Molitor’s shop, the Police help me get my car back.
Feb09 The fabulous gents of SpecE30-SE, in an epic adventure, help me (they did most the work) replace the motor that Molitor hosed up with a junkyard motor at the track. It took us 4hrs.
Feb09 My junkyard motor turns out to be a weak POS.
Mar09 My junkyard motor can’t hold oil pressure.
Mar09 I start rebuilding the Molitor motor and I buy a brand new head. But when the head arrives it does poorly on compression and leakdown tests. I spend weeks installing and testing my 3 heads, because I assume that I’m messing up the compression and leakdown tests. After a dozen iterations, I became the fastest E30 head installer in the world today.
Mar09 I gouge the deck of my new head so I have to take it to a machine shop and get it decked.
Apr09 After arriving at some comfort level that my compression and leakdown tests can be trusted, I try a drip test on my heads. After many long conversations with the folks that built the head I send it back to them over their objections. They call back later and say the the head was indeed messed up.
Apr09 I get the head back and have a local shop help me with the build of the bottom end. They build it with a little assistance from me, and conclude that a main bearing has too much clearance and the crank has to be machined to fit an over-size bearing. After talking to the machine shop at length, I build the bottom end myself and the clearances turn out fine.
May09 I fail to install a head locating pin that goes on the block’s deck and the head doesn’t get positioned just right. The result is a slight pinging noise. Having seen 3 “pro’s” put on heads without the pin I just didn’t think that it was a big deal. Having installed the motor into the car myself, I take the car to the shop to figure out the pinging noise. They charge me >$1k to figure out that the pin is missing and a piston head was just ever so slightly whacking the head and making the “ping”.
When the local shop removed my head the rocker arm shaft retaining pin popped out and no one noticed. I put the head on the motor and go to RA and race with my fabulous engine and the head fails because the rocker arm shafts rotated. My $2k head is ruined.
May09 The shop that built my head are great Americans and they build me another head at cost. I install it and drive on. Later dyno results are a little disappointing for a new head on an 0.020 motor, but I’m beyond caring.
Dec09. The coolant hose on the block near the starter failed. Coolant temp gauge didn’t really give much warning because once you lose some coolant, the sensor is no longer touching coolant flow. There’s something for us all to think about there. It was the oil temp gauge that told Simon that there was a problem.
When I had the motor out last Spring I had considered tapping the block and putting in a bolt to delete the hose entirely, but I had instead just cut it at 5" and blocked it off with a bolt and hose clamp. The hose failed at the block.
That’s as much history as I have the patience to type.